Retromaster’s Electronics Projects

…related to old computers and other assorted stuff…

Posts Tagged ‘Proxxon MF70’

MF70 CNC New Drive & Motors

Posted by retromaster on April 11, 2011

Here is the new motor driver installed and working with the new steppers. It is the infamous 3-Axis TB6560 Chinese driver commonly found on ebay. I could have designed and built my own, but the price was too attractive to pass up. The board supports 1/16 microstepping and 3.5A per channel @ up-to 36V supply. Combined with the new motors (Minebea/Astrosyn, apparently salvaged from Diebold ATMs) the speeds have more than doubled-up, at slightly more than 200mm/s.

The enclosure (from a local supplier) is of good quality, but ultimately an overkill, and it is a bit too large for this board. Unfortunately, the nearest size in the manufacturer’s catalog was just a couple of centimeters smaller than the board.

Despite all that looks good on paper, I have to be wary of recommending this driver board, because mine turned out to be defective! Upon testing, I found out that the Y-axis was not providing enough torque. Some inspection with a multimeter revealed that the DIP-switch for the Y-axis was broken, resulting in the current setting being ignored. The fix was easy, with just a couple of wires, as in the photo above. Nevertheless, this just seems like another example of fine (!) Chinese manufacturing on display.

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Upgrading the MF70 CNC Part 2

Posted by retromaster on April 5, 2011

As one may guess from the photos above, the polyamide endplates did not work well at all (and that is an understatement). So I had to switch back to aluminium, as it is still rather inexpensive and in the end I was not sure if even Delrin would be rigid enough in this case. As a matter of fact, Alcofribas had suggested that I use brass instead. I might have taken that route if I did not already have some alu in hand. Brass seems to be more expensive and quite a bit heavier than aluminium, but apparently it is machined dry. My setup is rather poor in handling the coolant generally required when milling aluminium, so this would have been an important advantage.

Having to go back to aluminium motivated me to do some research in milling speeds and feeds and coolant types. I found out the MF70 spindle was powerful enough to take deeper cuts in aluminium (1.5mm vs. 0.5mm) at my current feeds (about 90mm/m and 8000rpm). Apparently these numbers are still far from optimal, but they were a big improvement over my previous setup, which took far too long to mill the parts and caused the spindle to overheat pretty quickly. If the MF70 spindle horsepower permits, I plan to even further increase feeds (once I upgrade the steppers) to see how far I can take this. I can also confirm that ethanol performs quite well as a coolant for milling aluminium.

Another “improvement” was that I finally managed to obtain a dial test indicator, thanks to ebay. Measuring the backlash on all axes, I found it to be around 0.1mm, which is not exactly low, but easily compensated in software. In fact, this performs so well that I may not even bother to implement the split-nut anti-backlash nut design I was referring to in my previous post.

Finally, even though the new parts came out quite nice, the performance improvement with the old steppers was marginal. So, I decided to give priority to upgrading the steppers and the drivers over upgrading the mechanical parts. Depending on how that goes, I will decide if it is worth to actually rebuild the Y and Z axes.

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Upgrading the MF70 CNC

Posted by retromaster on March 16, 2011

Here is a new post after a litte hiatus.

First of all, let me get the Cumulus news out of the way: Last week, I’ve mailed the very first Cumulus board-set to ibisum for testing. He has five Atmos machines and the necessary hardware for debugging if things do not go as expected, so he is the right guy for testing at this stage. If everything goes smoothly, then I may think about organising a small production run for people who have expressed interest in purchasing Cumulus boards.

And now back to the main topic of this post. For various reasons, I decided to upgrade my MF70 CNC implementation. The aim is to fix some mechanical problems found in my original design, as well as upgrade the motors and the electronics to achieve higher speeds and precision. I even plan to try a split-nut anti-backlash design at some point.

The image above shows the very first parts I’ve manufactured that are intended to replace the current endplates in the X axis. As is evident from the photo, I’ve opted for using plastics this time, instead of aluminium. Although aluminium looks far more impressive, the plastic material I use here (specifically polyamide/nylon) is much easier and quicker to machine (deeper cuts, no coolant required, etc.) with a nice enough finish and they seem to be strong enough for the application (the original parts that come with the MF70 were plastic, too). In any case, if I find that the manufactured parts do not perform to my expectations I can always try out Delrin instead :).

These parts are very similar to the current aluminium parts but there are some differences. The mounting holes have been made into slots for allowing better alignment of the leadscrew with the leadnut. The bearing housing contains an additional 14mm inner groove to allow me to test thrust ball bearings (much higher axial load capacity) instead of the standard ball bearings that I’ve been using so far (I can still use the ball bearings if for some reason I am not happy with the thrust bearings). The motors will be mounted using an additional plate bolted to the motors. That plate and the larger plate in the photo above will be bolted together with a couple of M10 steel screws using the holes on the sides.

Posted in Projects, Retrocomputing, Robotics | Tagged: , , , , , , | 4 Comments »

MF70 CNC Page Up!

Posted by retromaster on February 16, 2010

I’ve put up a page that describes my Proxxon MF70 to CNC conversion. It contains photos (most of which were already on my blog here), schematics, drawings, board layouts, source code, etc. You can see it here.

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Y and Z Axes Version 3

Posted by retromaster on February 8, 2010

Here are the final versions of Y and Z axes of my CNC-converted MF70. The Z axis end-plate consists of two 5mm thick aluminum plates bolted back-to-back. One ball bearing is mounted in each plate, held in place together with the tightened nylon-insert nuts on the leadscrew. To clear the ball bearing on the bottom side I had to raise the end-plate using two nuts as spacers (not shown in the photo). I’ve also replaced the coupling with the new flexible one. It looks and performs considerably better than the previous version.

In the previous version, the Y axis leadscrew was supported at both ends. Instead, I decided to switch to a single side support scheme similar to the Z axis. This has the advantage that, on the other end, the carriage can move all the way to the Z axis column. I had to mill a new standoff for the end-plate in order to make room for the second ball bearing. This standoff is screwed to the lower table base to make it sit perfectly flat. To make sure that the single side support does not cause an issue, I’ve also built a new delrin nut that is a bit taller one one side than the original one, so that it tightly sits and slides on the lower aluminum base of the table, creating kind of an additional support. Overall, this new version of the Y axis is a very good performer and the travel has been extended to around 92mm, effectively doubling the stock MF70 travel.

For the moment, minor corrections and improvements aside, I consider the machine complete. In the future, perhaps I may switch to higher torque motors and more sophisticated drivers to improve on speed and smoothness. My intention now is to put together a project page to document the final state of the machine and provide some technical information, schematics, drawings, etc.

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X Axis Version 3

Posted by retromaster on February 3, 2010

Here is the third and hopefully final version of the X axis. In addition to installing the latest parts I’ve milled, I’ve also replaced the couplings with flexible ones from my previous post. There was not a big improvement speed-wise, but this new X axis is quite a bit more reliable and robust than the previous versions. Not to mention that it looks a lot better, too 🙂

Next, I’ll be working on the Y and Z axes. I haven’t yet made a version of the Z axis with ball bearings, and the Y axis could still use some improvements. There is still some work to do, but I think I am getting closer to completing this project.

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Software is important

Posted by retromaster on February 1, 2010

To the left of the photo above is the latest part I’ve milled using the MF70 CNC. It’s for the third version of the X axis, out of 10mm thick aluminum. It turned out very nice, but I’ve had to solve some problems before getting this result.

First, the X axis started missing steps randomly, then after a short while it stopped moving altogether. It was definitely not a mechanical problem, so after a little bit of debugging the drive circuitry I found out that one of the optocoupler chips on the breakout board had died. Replacing that chip solved that problem.

The next problem was even more critical that it actually ruined a couple of workpieces until I found about it. I was using a very popular piece of CNC software that runs under Windows XP. However, apparently, it was missing steps! I first noticed the problem when I saw that the two circles that form the bearing housing in the middle were not concentric. I did a test, by issuing a “goto to zero” command after milling the first circle. It was off by almost half a millimeter in both X and Y axes. This behaviour was reproducible and I did not think that it was mechanical. So, I installed EMC2 (together with Ubuntu) on the very same machine. Milling the same part with EMC2 gave the perfect results in the photo above. I suppose that the EMC2 installation coming with a Linux kernel patched with realtime extensions may have something to do with that.

I also found locally some good quality flexible couplings for a reasonable price. I’ll use those for replacing the (rather poor) rigid couplings I am using right now. They have a 6.35mm opening on one end with fits the motor shafts perfectly, and the other end is 4mm. So, I’ll need to machine the leadscrew ends to meet that diameter, but that’s not a problem.

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Assembled the New Stepper Drive Box

Posted by retromaster on January 27, 2010

Here is a photo of the new stepper driver assembled in its box, along with the laptop power supply I use to power it (and the steppers). The parallel port connector, power input and power switch are in the back. Now that the new driver has made the machine much faster, it’s become a lot more fun to use it :). In addition, with all the little improvements like the new connectors and the advanced PC software control, it has become much more reliable, too. Since the motors do not draw a lot of current, the box does not seem to get very hot (not that it’s difficult to rectify in case that happens). Now I’ll go back to improving the mechanics of the machine, as there is still some work to do in that area.

The faces of the box were cut using the CNC itself. One thing I found out (!) was that using a 3mm cutter at a high RPM to cut ABS plastic does not work very well. It melts the plastic and leaves a terrible finish, not to mention the melted plastic sticking to the cutter. I had to switch to a 1mm cutter, reduce the RPM, and make sure that the whole thing stays cool. This way I was able to get perfect cuts.

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New Stepper Drive Boards Ready

Posted by retromaster on January 26, 2010

I’ve finished building the new bipolar stepper driver. I’ve tested it, and it works, with a big speed/torque increase. There are two boards, a parallel port breakout board (with optical isolation) and the actual stepper driver board that accepts step and direction pulses. As I’ve mentioned in previous posts, I’ve gotten rid of the current sensing resistors and gone for a fixed frequency PWM chopper scheme instead. This seems to be sufficient for the motors I currently use, but I am definitely interested in trying out more elaborate driving schemes with more capable (higher current, lower voltage) motors in the future.

Both boards are designed to be mounted in the plastic enclosures as shown in the photo. There will be a 4-pin round connector for each axis and a power led on the front side of the box. On the back side will be the parallel port and power connectors as well as a power switch. I might also put some ventilation holes somewhere on the box but I am not sure that they will be necessary. Cutting the plastic plates for the sides of the enclosure will be the first order of business for the new drives.

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PCB Drilling with the MF70 CNC

Posted by retromaster on January 11, 2010

Over the weekend, I worked on getting rid of the backlash in the MF70 CNC. I’ve made new delrin nuts that fit much more tightly in the nut housings and I’ve tightened the stop nuts on each side of the X axis to make sure that there remained no play in the ball bearings. As the first photo shows, this resulted in a huge improvement in the backlash situation, although I had to reduce speed as the X axis became more difficult to move. Also, something I noticed before but I neglected to mention in my previous posts is that the X axis endplates do not seem to sit perfectly flat on the sides of the table. This may be because they are getting bent when the mounting screws are tightened. I think I may have to try rebuilding the endplates using aluminum twice as thick.

In addition to fixing the backlash, I greatly increased vertical speed for drilling and shortened the extension of the drill bit to just a few millimeters below the chuck, eliminating most of the problems due to wandering and flexing of the drill bit. But even these improvements were not enough to get a perfectly drilled PCB. It seems that warpage of the copperclad introduces a significant error as well. So significant in fact, that the holes in the top board in the first photo above did not align properly with the printout of the PCB layout. I also found out that I needed to have the hole locations mirrored since I was drilling from the copper side (this is a single-sided board). So I came up with the drilling setup in the right photo to fix the warpage issues and I had the hole locations mirrored, and I managed to have a drilled copperclad that matches the PCB layout very well.

The PCB I building is for testing the new axis drive circuitry that I mentioned in the previous post. In a few days, I expect to finish making and assembling the PCB. After a little bit of PIC coding, I’ll at least have an idea of the torque increase I’ll get from the new drives. If it turns out to be as worthwhile as I think it’ll be, I’ll build a new board with all drives for all 3 axes and then go back to improving the mechanics of the machine.

Posted in Homebrew PCBs, Projects, Robotics | Tagged: , , , | 4 Comments »